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Nominee
Curbing production wastage
Motherson Sumi Systems, a manufacturer of wiring harnesses
for the automotive industry, was finding difficulty in handling the end-to-end
production life-cycle process. the company was experiencing extensive wastage
of raw material and delay in order delivery. In order to overcome these problems,
the company went in for automation that helped in increasing productivity and
RoI
Though the company had in place a cutting & crimping (C&C) machine
that looked after various processes like wire cutting, wire stripping, and seal
insertion, it needed to set up another C&C machine for jobs based on various
parameters such as wire length to be cut, size of the terminal and crimping
force. Hence, the company was looking for a solution that would not only automate
the machine set-up process, but also bring accuracy, efficiency
and profitability.
Identifying the problem
Because the cutting and crimping of wires has to be done in large numbers and
the C&C machine was the only machine to perform all the critical tasks,
it was prone to errors that led to extensive wastage of raw material and delayed
order fulfilment.
This need was ITtaken up as a process improvement drive by the IT team
in February 2005. It was realised that by simply automating these areas, the
process could be made mistake-proof, and the machine set-up time could be reduced
thereby saving in material wastage and enabling increase in productivity,
says Vandana Avantsa, CIO, Motherson Sumi Systems.
While analysing the process for probable automation, it was found that
there was a lot of manual calculations and data entry of the set-up data for
the C&C machine. This made the process error-prone leading to extensive
wastage of raw material (copper wire, terminals, etc) and delayed order fulfilment,
adds Avantsa.
Making the right choice
After identifying the real pain areas, Motherson thought of automating the machine
set-up process. It chose the Shop Floor Control System (SFCS) for the same.
The SFCS envisages automation of the machine set-up process, aligning
of the processes to increase productivity, mistake-proofing of wrong raw material
usage and raw material batch traceability.
Technologies deployed were Bluetooth bar code scanners, adjustable sensors,
controller, voltage regulators, bar code technology for utility and .NET base
application for Daily Work Report.
The main challenge faced was the integration of software solution with C&C
machines and user training and availability of production machines for the final
testing. Moreover, at the time of integration testing, there was a need
to have the production process available to the IT team, which was critical.
To meet these challenges we did the testing job only during off-production hours
(lunch breaks, shift changes, etc), she adds.
The unique factor
With the scan of a bar code on the instruction sheet at the cutting & crimping
machine, set-up data gets automatically populated from the ERP upstream modules.
Actual observations are directly transferred from equipment such as the micrometer
and push-pull tester in the application. The company claims that data received
is 100 percent accurate as there is no manual intervention.
In addition the solution provides machine life data for planning
and scheduling preventive maintenance. Alerts related to the C&C machine
maintenance parameters are sent by the system to the maintenance department
through e-mails.
Unlimited benefits
With an investment of Rs 10.21 lakh and ongoing cost of Rs
3 lakh per year, Motherson achieved a good RoI and savings after the project
implementation. The companys return on investment is 620 percent and savings
per machine work out to Rs 1.58 lakh. Overall savings with respect to 40 machines
is Rs 63.34 lakh and over the next three years the company is confident that
the initiative will reduce costs by Rs 2.5 crore. Expense reduction as a percentage
of revenue is 0.0624 percent.
Road ahead
With the present solution deployed, the company is planning
to create a dashboard atop this application to assist supervisors, plant heads
and top management in decision-making. The design phase is underway and go-live
is slated for December 2006.
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